Saturday, 27 November 2021

NEAL 102 & 103

 NEAL 102 & 103 Transcription Cassette Decks


Taken from the 1976 HiFi Year Book.




Saturday, 2 October 2021

AKAI CS-705D

The AKAI CS-705D

Original ebay Advert Images of the CS-705D.
 

Advertised for 'parts or not working", I got this little attractive looking deck up and running in less than 30mins.

However, there's much work to do on it - the record head was quite thick with dirt and oxide, and the pinch roller looked as if it hadn't been cleaned for decades. The CS-705D was a little corroded internally in places, but in fair condition. The VU meters were misbehaving on Play.

So far ...

  • Removed internal debris
  • All contacts and switches cleaned with Servisol Super 10
  • Capstan shaft lubricated with Revox recommended capstan oil. 
  • Pinch roller - removed all tape oxide with diluted acetone, later isopropyl alcohol, and finally water. Roughed-up surface by rolling pinch roller on fine grit paper, removed excess rubber (vacuumed), then applied some Rubber Renue.
  • DC Motor (dated Nov 1976!) removed, applied Servisol Super 10 down the shaft. The fitting appeares to be standard, and so a replacement may not be difficult - looks like a 2mm spindle? 
  • Cleaned associated motor pulley.
  • All muting and similar switches cleaned.
Measurements -
  • Erase head bias frequency/voltage: ~85Khz/~35v peak.
  • Record Head bias frequency/volatge: ~85Khz~9v peak.
 Observation -
  • Electrolytic capacitors seem good, may replace later?

The deck is now functioning, recording, and playing back almost as new.

Issues to be Addressed

  1. Record/Replay Head replacement or lapped? So far - recording and playtback are fine, much better than expected, but the head wear is obvious. 
  2. Motor speed seems to drift over time?

11/10/2021

A New Record/Playback Head Installed

Original Record/Playback head -

This doesn't appear to be the original P4-303 or
HN-424822 record/replay head?
Head wear is actually deeper than it looks in this photograph.


Although the old head worked well it had obviously done some miles, so I chanced a few potential replacements. Looking at the two 'new' heads I bought, and the original head fitted in the CS-705D, I decided to perform some measurements.

The results are listed here ...

(a) Original: '512 K6AB', R ~ 192Ω, L ~ 110mH (at 10Khz)

(b) New: 180-T1905, R~250Ω,  L~ 78mH (at 10Khz)

(c) NOS: 445-20 E S1X10, R~ 350Ω, L ~ 127mH (at 10Khz).

Again, I suspect the 'original head' was not the exact one that came with this machine back in 1976? (Edit: It may indeed be the original, as other images of the CS-705D on the internet show the same record head identity number.)

Head Capacitances: While it is true that the inductance value L should be independent of excitation frequency, we have to appreciate that a record head also has parasitic capacitances, which is why (I suspect) that the apparent measured inductance varies a with test frequency?

Before I decided to replace the head, I measured (under load) the peak head bias frequency voltages in record mode on the CS-705D. They were ...

Type I (Normal Tape): default 9v, (can be varied from 5v to 18v)

Type II (CrO2): 14v, (can be varied from 7.5v to 26v)

Type III: Fe-CrO2: 12v, (can be varied from 7v to 24v)

 

Calculating 'Normal' Bias Record Head Current

From Ohm's Law, we have I = V/Z, and for our existing record head the impedance at approximately 85Khz is going to be -

where Z = {R²+(2πfL)²} ~ 59,000

It should be noted that the impedance from the inductor L is frequency dependent and dominates the overall impedance Z.

From this 59KΩ impedance, both peak and RMS bias current can be estimated -

Original '512 K6AB' Ibias ~ 0.15mA peak, or 0.108mA RMS.

Ibias is the high frequency bias current that will flow through the head, even when there is no signal applied during recording. Any additional audio signal added to the bias is very small in comparison.

Which 'new' Head to Choose?

Good question - I don't have the defintive answer, but I decided to try the 180-T1905 first. At 85Khz, its impedance was going to be lower since its inductance was less.

Ignoring the internal DC resistance for this calculation, Z ~ (2πfL) ~ 41600Ω, and so the bias current from the 'new' 180-T1905 head can be calculated, and found to be 0.15mA - almost identical!

After fitting the 180-T1905 head, all that was left to do was to - demagnetise the head, re-set the azimuth, re-calibrate PB levels (from a Dolby Level reference tape), adjust the internal record levels so that 0VU on record, gave back 0 VU on playback. And then finally alter the bias (actually bias amplitude!) from the potentiometers on the circuit board.

Success? ....  yes, excellent!

The AKAI CS-705D records and plays back very well indeed. It's 333Hz and above frequency response is almost flat to 13,000Hz, and about -3dB down at 15,000Hz. This is better than the original specification.

I haven't yet arrived at the point where I will undertake a full frequency response test, and weighted signal to noise ratio assessment.

Track Height Adjustment?

Possibly later I will add a fine shim and test for true track height alignment using one of my Nakamichi 3Khz track height test tapes.

 
14/10/2021: Both with, and without a shim added, I measured the output peak-to-peak from a 3Khz Nakamichi-DR10-made track height test tape. The difference was small, but with the added shim the playback amplitude was slightly greater. The head tape guides are now truly equidistant from the tape. So the shim stays in!

Motor Speed Variatons.

As mentioned above, the motor speed controller appears to let the motor drift off speed. It's not serious, so I will look into subject at another time. 11/10/2021.

14/10/2021: Old Motor Refurbish Attempt

I took the old motor out, and stripped it down to the bare motor assembly, then fired some more Servisol Super 10 down into the armature/stator chamber, just to be sure its truly contact cleaned! 

Also, as a precaution I desoldered two electrolytic capacitors on the motor speed conroller board, then replaced them with new 3.3uF and 4.7uF capacitors.

All re-assembled, and (so far) working well. Again, I speed-calibrated the motor, so only time will tell if I have found the source of the problem?

 

Motor Casing.

Note: There is a removed sheath that electrically
isolates the casing - not shown.


DC Motor Controller Board - can be removed by desoldering at X-points.
Note: Polarity is important, otherwise the motor will run clockwise
- currently, it runs CCW (counter clockwise).

The best way to de-solder is to use a copper braid which 'soaks up' the molden solder during de-soldering.

14/10/2021: The motor was again starting to drift in speed, in a similar manner to the motor that was originally in the AIWA AD-F770 - the change was slow but noticeable.

15/10/2021: New Motor Fitted
 
Mabuchi (a copy?) CCW 2400rpm motor now fitted.
Runs off 12.6v DC supply, 12.6v under load conditions.
 
Played the CS-705D for more than an hour - all working well, stable sound. 
 
Motor Speed Drift 17/10/2021: The speed seems to drift again - it's very subtle, but noticeable. Confirmed this when I had to recalibrate the speed using a 3Khz calibration tape - twice. So I am not imaging it! 
 
Power supply is stable, so my attention is on (a) the new motor, (b) pinch roller and possible slow motion slippage? (c) Excessive belt tension? - motor load current is higher than expected Play=ON ~150mA, FF=ON ~260mA, RW=ON ~250mA! 

Comparing DC Motor Load Currents
 
Here I've compiled a small table of results comparing DC motor load currents with a TDK D46 tape inserted. 
 
Bare in mind, the torque (Torque = tangental force x radius) developed by a motor is proportional to current, ie T ∝ I. Example: A doubling of armature current is required to drive a doubling of load torque.

Cassette Deck Model

Play Current

FF Current

RW Current

AKAI GX-M10

~ 57mA

65mA … 74mA

59mA … 106mA

NAD 6050C

~ 68mA

72mA … 90mA

71mA … 120mA

AIWA AD-F770

69mA ... 75mA

NA

NA

SANSUI SC 1330

~ 54mA

98mA …135mA

103mA … 170mA



AKAI CS-705D

(before belt stretch)



~ 150mA



200mA

± 50mA



250mA

± 50mA



AKAI CS-705D

(after belt stretch)



120mA ... 125mA



200mA

± 50mA



250mA

± 50mA


We can immediately see that the current required for the CS-705D is more then twice that for other machines. Indeed, after deliberately and uniformly stretching the flat drive belt in the CS-705D, I was able to bring down the average Play current - but this is still too high.

I can only conclude for now, that the loading on the small DC (internally speed regulated) motor is beyond the specification of the motor!? Hence the reason why its speed 'wobbles' or drifts as it gets warm. Or is it more likely that the motor and internal speed regulator circuits are failing?

New Old Stock (NOS) Motor: Matsushita MMI-6S2LS

29/10/2021 

After trying several NOS (New Old Stock) 12V DC motors (a genuine Mabuchi, and a 'Mabuchi' Chinese copy), I finally installed a 1994 unused Matsushita MMI-6S2LS. All motors of course include their respective motor speed controller circuits. 

After 2 hours play, no problems to report, and no large current drainage!

  

The torque now demands currents of -

Play: 76mA ... 83mA, FF: 150mA ... 180mA , RW: 150mA ... 200mA

The above figures are dependent on which spools have the most tape on them. Any excessive tension applied by the belts will also increase Play, FF, and RW torque currents. 

One fact that struct my attention, was the internal 'slip' friction (and additional torque load) demanded by the take-up spool. The CS-705D has a strong take-up spool force, which when in Play mode, adds about 20mA. This means that when in Play + Pause mode, the dc current is only about 57mA/58mA.

Speed Calibration

Using an ABEX 3150Hz reference tape and frequency counter, I have the deck set up to playback somewhere between 3150Hz and 3160Hz - which is slightly fast.

Hopefully, this time the motor speed won't start to drift!


********************


Note: Long exposure photograph.

31/10/2021

LED Illuminated VU Meters

I decided to change the old filament lamps for white LEDs. However, the original lamps worked off a transformer ac tapping, whereas any new LEDs in circuit will need DC to get them working without flickering.
 
The proposed modifications and circuit is - 
 
 

 
VU Meter LEDs ready to be used.
Note: all exposed wires were electrically isolated
after this photograph was taken.

The LEDs now in circuit are not working to their full brightness, they don't need to. Two LEDs in series for each VU Meter is sufficient, where each LED is only consuming between 6.0mA and 6.3mA. Some 12.4mA of dc current was observed which will split into approximately 6.2mA x 2, since this is a parallel circuit. 

The two original 1000uF (25v rated) electrolytic capacitors were replaced by larger 3300uF (actually ~2900uF) capacitors. The idea behind this was to increase the available charge for both the 'new' DC motor, and Q1 voltage regulator circuits.

As a matter of interest the AC fuse currents were measured at F2 and F3 - they were approximately 188mA (before the LED circuit was introduced), and about 107mA for the DC motor circuit in Play mode.
 
All working well - very nice bright and clear VU Meters!
 

 
Cassette transport speed is still very stable!

Other Images
 

 


Playback EQ (De-emphasis) Modification (12/11/2021)

A small change to the playback (PB) equalisation circuit and curve was made to help compensate for any new record/playback head that I fit.
 
All electrolytic capacitors in the area were also replaced.

The resistor R12 is now a 20kΩ variable trimmer
potentiometer set to about 10kΩ by default.


 
AKAI Record/Playback EQ
 
I do not have any Akai alignment tapes, so the earlier record and playback EQ specification adopted by Akai is unknown, but I can assume it probably approximates closely to a 1970s IEC standard, but with slight modifications to suit their designs and record head constraints? The same probably applies to Sony, Pioneer etc?
 
Using a Home Made IEC 1981 Reference Tape
 
Using a home-made (approximate) IEC 1981 specification alignment tape using the Nakamichi DR10, I set the playback response of the AKAI CS-705D to approximately -6dB at 10Khz in comparison to the output at 333Hz/400Hz.
 
Why -6dB at 10Khz?
 
Nearly all the (pre-Prague 1981 IEC standard) second hand decks that I've bought exhibit a -6dB (±2.0dB) output drop at 10Khz (reference to 315Hz/333Hz/400Hz levels) when playing back the home-made IEC 1981 reference tape, created with the Nakamichi DR10. 
 
Since my Nakamichi DR10 has not been used extensively, I feel reasonably confident with the general accuracy of this setup. To support this proposition, my (post 1981) Revox B215 and even a humble Marantz SD-35 follow the Nak DR10 playback curves reasonably accurately, to within ±1.5dB at 10Khz.

Just to reiterate, I simply use the Nakamichi-made 'IEC 1981' tape as a general playback guide at 333Hz and at 10Khz only, it is not a reference tape for older pre-1981 machines.


Article is subject to small changes, additions, and corrections without notice. 14/11/2021.


cassettedeckman@gmail.com

Tuesday, 28 September 2021

NAD 6050C

 The NAD 6050C Cassette Deck

(When this article is finished, this notice will be deleted.)

I admit, I've become a cassette deck addict - I simply want to fix them! I buy them cheap off ebay, but always first assess their build quality, potential present, and potential future faults before bidding.

My latest repair job is this NAD 6050C front loader. Like many, it was advertised as 'Spares or Repair'.

The date of manufacture was 1984, as stamped on the motor.

Initial problems

  • Dusty and dirty internally, but mainly in the cassette tray
  • Disintegrated belts - new belts fitted.
  • Noisy DC Motor - cured with Servisol Super 10 injected down the neck/spindle of the motor.
  • Inert or sticky transport - isopropyl and Servisol Super 10 freed, and cleaned the mechanisms. Some PTFE spray and silicone grease applied where necessary.
  • Cassette tape guide and hold latch - see below.
  • Inconsistent output - Servisol Super 10 applied to all potentiometers.

All the above have been fixed.


Now fully working: The NAD 6050C


Previous Findings:



The cassette guide and plastic latch on the right hand side was repaired - it had developed a small, almost unnoticeable fracture which weakened the spring action. I super glued the fracture - opening the fracture to allow glue to work into the crack. A small, cut piece of aluminium acting as a support bar was also bonded underneath to support the stressed area.

Now the spring action of the latch is 'springy' and strong.


 

Tape Wrap across the Erase, and Record/Playback Head


 

The Power Supply

Quite simple - a mains switch (no suppressor capacitor present), then a fuse into the primary transformer windings.

More to follow later ...

 
New Belts Fitted
 
After the mechanism was cleaned and lubricated, new belts were ordered - all working well. 

Rewind Problem


 
It is important that the compression from 'pulley 1' is high, as this also pushes the gearing for REW (rewind) into place.
 
Pulley 1: I initially fitted a belt that worked, but the gears did not  always engage quickly. Later a smaller (and tighter!) belt was fitted, and now the problem has disappeared. (correction made)
 

8/10/2021.

Monday, 14 June 2021

Revox A77 Servicing

 The Revox A77 MKIII

 

This blog/article is a work on the progress of servicing my 1971 Revox A77. It will be periodically updated, amended, and corrected until it is finished. When finished, this paragraph will be erased. (02/07/2021)

A factory stamped 'November 1971' Revox A77 that's been in the family since 1972.

The same date was also originally stamped on the heads.

This blog/article is intended to be a servicing account, let's see how far I can go?

Last time I switched this on was around 2003-2005. Before switching the machine on though, I checked that all three motors (Reels, and the capstan) were turning smoothly, other internal mechanisms ran/moved smoothly, contact and switched cleaned here and there, and finally changed some potentially dangerous capacitors that are known for catching fire.

14/06/2021: Report so far - it's working!

Playing original AGFA PE36 Tape.





Inside rear view - before any capacitor replacement.


Initial Inspections
 
Headwear and Guides
 
Record/Replay Head wear: the flat spots are quite wide.
Tape Lifter: small amount of wear, but may need replacing.
Erase Head: No signs of wear
Left Tape Guide: Runs smoothly
Pinch Roller: Free running and cleaned with Rubber Renue *
Capstan Shaft: Cleaned *
(*after this picture was taken)

 

 

 

 
Reel Motor and Spindles
 
I checked the free movement of the reel motor spindles - they spin easily with no apparent excessive internal friction. The shafts will be cleaned and lubricated later.
 


Some Initial Capacitor Replacements

Tape Drive Board: I initially replaced the said board's capacitors with metalised polyester 0.47uF 250v dc units, but later changed again to 0.47Uf 275 vac 'safety capacitors' in yellow. I'm not sure if there's any benefit to this, but it seems to be the general consensus?
 
Actual units in the Revox A77 now in yellow.

Originally -


Initial replacements -



Power Supply & Regulator Board.

The old original 2500uF canister type electrolytic capacitor has been replaced by a 3300uF 50v rated device - shown at the rear. A blue radial JB type is a 1000uF direct replacement for the old 1000uF axial type. 
 
I hope later to replace the '2500uF' original with a KEMET 100V 3300UF ALS31A332DB100. This has a high ripple current rating. 
 
An old 3.3uF tantalum (not shown) in the regulator circuit side has also been replaced, but by a standard aluminium electrolytic. All replacements have higher voltage ratings than their older counterparts.

There are two dc power supplies on the A77 -
 
(1) A 27v dc circuit containing the 3300uF capacitor is the only form of 'regulation' and/or smoothing which serves the transport relays, solenoids, power and meter lamps.

(2) A 21v dc regulated circuit where the 1000uF capacitor resides and serves its purpose for  - audio electronics, capstan motor speed control, and the end-of-tape lamp.


These are the initial and probably necessary replacements before I could be reasonably confident of working the deck. There are no 'running hot' issues at all.
 
Getting the Revox A77 up and running has given me a good measure of confidence to playback some early mono 1960s recordings made by my father that I wanted to digitise.
 
So far the Revox A77 is stable, and generally working well.
 
I'm aware that there are several issues to address:
 
  • Complete the re-capping of all electrolytic capacitors, including tantalum types. (Most completed 2022)
  • Main potentiometers to be replaced. (All but one replaced, 2022)
  • New Motor Run Capacitors. (Done: 01/07/2021)
  • End of tape switch off issue
  • Tape guide bearings may be improved by replacing? (Replaced 2022)
  • Reel brakes cleaned, better than before - re-clean?
  • Tape lifter may need replacing or modifying?
  • Reel motors may need some lubrication?
  • Capstan motor may need lubrication?
  • Bias trap band-stop filter refinement? (Done: June 2021)
  • Bias amplitude trimming to obtain a frequency response 30Hz .. 16Khz ±3dB at 9.5cm/sec.
  • New Record and Replay 1/2 track heads? - will need to create an azimuth tape, and calibrate playback levels from a known reference tape.

Bias Traps

A 120Khz high voltage 'bias' frequency generator on board the A77 is a neccessary building block to successful analogue recording on tape. A bias 'carrier' voltage is applied to the record heads, and the recorded signal (music. speech etc) 'sits' on top of this 120Khz bias signal. This modulating scheme is similar to Amplitude Modulation 'AM", although it is not mathematically the same. The result of applying a bias carrier is a linear, low distortion magnetic field image of the audio transfered to tape.

However, some parts of the overall A77 circuits need to be isolated from this 120Khz bias carrier, and so Bias Traps are employed - in particular, the recording, and playback amplifiers.

 

Underside of Revox A77
The Bias Traps for Record, and Playback circuit
access points have been opened up ready for fine tuning.


The recording circuit schematic is shown below, and a test point is established for adjustment of the bias trap. The bias trap is a standard bandstop filter where at approximately 120Khz, the inductive and capacitive reactances are (theoretically) opposite and equal in phase. It is at this resonant frequency where the impedance of the LC circuit is theoretically infinite, however, in practice owing to small internal resistances and leakages this is never attained, but is sufficient enough to work well.

The Record Amplifier Schematic
I later traced and then marked on the underside of the board
a point where I could use an oscilloscope probe.


Trapping the Bias Signal: Record Circuit

Pressing Record and Play initiates the record circuits and the bias carrier is generated. Turning the small trimmer choke L501 (for CHI on card CHI, and CHII on card CHII) with an insulated screwdriver I observed the 120Khz signal, and turned for minimum amplitude - it never diminishes to zero. At this test point, the minimum amplitudes for both CHI and CHII were down to approximately 50-75mV peak.
 

Trapping the Bias Signal: Playback Circuit

After engaging Record and Play again the trimmer chokes were adjusted for the playback circuit. The test point this time is at line out, ie at the phono sockets. And again, we aim for minimum 120Khz bias leakage voltage. The bias signal does not completely diminish.
 


With Ampex 499 tape wound on to the Revox A77, setting record and play set to ON, and with a 1Khz test tone applied at the input set to 0VU, the recorded 'NAB' playback 1khz output at line out was approximately 6v peak to peak. 

Below shows the oscilloscope trace showing the best 120Khz bias bandstop attenuation results (without 1Khz modulation) -

 Note the crossover distortion - probably due to the non-linear B vs I  charactersitics of the choke at low levels of excitation current.

As can be seen, the amplitude is approximately 100mV peak to peak (~35mV rms) on CHI and 170mv peak to peak (~60mV rms) on CHII. The best figure equates to approximately 20Log(0.1/6) ~ -36dB lower than the audio signal at 0VU.

Both original 390pF bias-trap circuit capacitors were replacd by newer 1% tolerances versions. 

Revox A77 Motor Run Capacitors

Employed to produce neccessary current phase shifts so that all 3 motors experience the correct rotating magnetic field phasing.

Old motor run capacitors in the A77 are known to be suspect, especially after 20 years and more, so I need to change these. So far I've had no problem, but it's best to be safe than sorry.

Old A77 Motor Run Metalised Paper Capacitors
2 x 4.3uF, 1 x 3.5uF


Just ordered new Ducati caps ...


New Motor Run Capacitors Fitted

New A77 Motor Run Ducati Capacitors: 2 x 4.5uF, 1 x 3.5uF
(Note the small difference: 4.5uF compared to 4.3uF)


Potentiometers Replaced

All but one of the onboard potentiometers were replaced earlier in 2022.

On replacement, first measure the resistances either side of the extracted potentiometer, set the new one to the same value, then replace.



05/12/2022: As the blog/article and work on the A77 is unfinished, there will be alterations and corrections made to the above.

cassettedeckman@gmail.com