Thursday, 14 November 2024

Technics RS-673 Cassette Deck

Technics RS-673 Cassette Deck
 

I saw this on ebay very recently, and I was hooked. This is a quite a rare machine, but before I bought it, I just wanted to be sure it was repairable as I mulled over all the pictures, and the description of this 1978 machine.
 
Original Advert
 

 
Before continuing, the reader might wish to know that there is no obvious or available service manual to the RS-673 as far as I am aware. If you know where I can find a service manual to this machine, then please do help, thank you.

Another Technics RS-671 has an available service manual, and much of what is in there applies to this RS-673 model, except for the fluorescent metering.

Initial Testing

I could see that the deck was 'basically' operational, but it would not Play, nor rewind (RW), nor fast forward (FF).

The transport mechanism has seized up - decades of 'dry' lubricants, a fine layer of dust, and enough oxidation to grind things to a halt stopped the deck from making any sound.

Before any other work was done, the transport had to be working, and so the top side of the transport was cleaned carefully.

The tape supply hub/spindle has seized completely, so much so that I could hardly move it with my hand! This was the reason why the auto-stop kicked into action once Play was pressed.

However, after injecting some OB41 freeing-oil down the spindle of the hubs and 'working' the spool a little with my hand, free movement was restored to this and the take up hub. The remainder of this side of the transport was taken apart and cleaned with a mixture of detergent/water, switch cleaner, IPA, and acetone. Note - take care when using acetone on plastics, there will be a chemical reaction with regard to some plastics and this will ruin the 'look' of the said plastic. Please check online for more details.

Later, all idler tyres were removed, cleaned, carefully 'roughed up', and with Rubber Renue applied, returned to their original postions.

Other concealed but essential sliding mechanisms had to be cleaned and lubricated too - 'renewing' the idler tyres was simply not enough to cure the problem of zero RW and FF!






 
 


Later, the pinch roller was carefully 'sanded', cleaned, and Rubber Renue applied, and then allowed to dry. Associated mechanisms were removed, and cleaned to allow free movement of the pinch roller.

Earlier on, both heads were cleaned with acetone, with special attention applied to the record/play head. There is obviously some wear, and as a result I am aware that this could impact on performance, possibly more in the right-channel (innermost track) more than the left-channel  (outer track)? The capstan and heads were also de-magnetised.

The flywheel was taken out for inspection, lubricated then returned and cleaned again as the oils ran into the sintered bearings and would probably transfer on to the pinch roller if I didn't clean this again!

Drive Belt
 
Estimating for now, the main drive belt is about 130mm in diameter, and about 5mm wide - this seems to have been replaced in 1996 and/or 1999? The belt will be replaced later, but at this moment it's fully operational and stable.
 
Basic Calibration

With already some 6 hours into this restoration project some basic calibration work was performed.

Before that could be done, all potentiometers, and switches were 'switch cleaned'.

Also, the bias traps were re-set to maximize rejection of the bias frequency 'carrier' - there are calibration points marked to do this.


After basic calibrations: Bias Trap, Azimuth, PB Levels, PB EQ, Record Levels etc, the machine at this moment is returning the following figures ...


Wow/Flutter: < 0.11% WRMS (more often under 0.10% wrms).
Speed Stability: WRT a 3150Hz ABEX reference tape, it is good at approximately ±2Hz after 10 minutes.
Frequency response: 35Hz ... 14,500Hz -3dB for Type I 'Normal' tapes.
THD: At +2dB or slightly greater above Dolby Level, it is approximately 1.5% at 1Khz.

Recording Level Instability
 
A small, almost un-trackable variation in recording level in one channel was sometimes experienced. This was seemingly fixed when associated electrolytic capacitors, and 2SC828 NPN transistors were removed and replaced. Possibly pre-emphasis was affected in a small way?
 
 


Observing the schematic above, it is quite possible that either one or both of the switching transistors were not functioning properly? When in record mode, they should switch into their saturation region, and offer a near short circuit for ac signals to ground.


So far, the Technics RS-673 is running very well.



This Blogger article is unfinished, and will be subject to corrections, additions etc without notice. [15th November 2024]

Wednesday, 9 October 2024

Technics RS-630TUS Cassette Deck

Technics RS-630TUS Cassette Deck

 
Lots of little issues with this 'faulty' deck that I bought off ebay. Cosmetically, it is in good shape.


Problems -
 
  • Stuck sliding door.
  • Stuck Front Panel Switch
  • No mains plug.
  • Worn pinch roller.
  • Slightly slippy belt. (Measures approx 86mm diameter x 3.5mm width)
  • Playback amplifier sporadic oscillations, mainly in the left channel.
  • Dust in cassette mechanism.


Most of the above were easy to correct, however the main concerns were - reliable transport functioning and the sporadic oscillations from the playback pre-amplifier.

Pinch Roller & Transport

At first the thought of replacing the pinch roller looked daunting, but later realised that the 2mm internal pin that holds and guides the roller could be tapped through from the bottom side.

Here's how - very carefully break the plastic cap at the dead-centre point with a very fine drill, screw driver, or punch (~ 1mm diameter or less), this produces a small opening, and then very gently 'tap-out' the steel pin.

A 13mm or 13.5mm diameter pinch roller will work, but a 13.5mm diameter roller is recommended as this will give a slightly higher pinch-to-capstan pressure.

My initial attempt cracked the underside
of the support for the pinch roller.
The strength of the assembly was not
compromised, but still I re-enforced
areas of importance.


The torsion spring that provides the pinch-to-capstan pressure is slightly puzzling. According to the Service Manual, the torsion spring is fed with its longer tail to the right as we look down on to the transport mechanism.

However, observing some online pictures, when in situe, the torsion spring needs to be tensioned like that indicated in red.


 

I have attempted to set up the tension like so, but found it extremely difficult, even with tools made for this kind of work.

So another solution was found.

The torsion spring is first centred underneath on the plastic pinch roller mechanism, and selecting the highest torque by 'pinning' the leftmost (shorter) spring arm into the relevant guide (hidden in this picture) should be done before returning the mechanism to the main board guide. The rightmost part can be secured into a groove provided by the Pause sliding parts.

 
Upper Left Side: This frontside view shows the torsion spring fully located - the short side of the torsion spring is tucked on to the underside of the roller swivel mechanism (as normal), and the longer tail is tucked into a Pause mechanism slot.

To increase working torque exerted by the torsion spring - first, the spring has to be carefull bent to increase effective torque.
 
Factory Torsion Spring Positioning

I may at a later date try again with the spring in its factory default set up, but the spring will have to be bent again allowing me to tuck the shorter side under the roller assembly arm.
 
Auto Stop Problem

This would not activate, and the reason was quite simple - the spinning rubber idler tyre was not turning with sufficient force to activate the autostop.

This idler works off the brass knurled section of the capstan/flywheel, and was currently providing too much slip. The idler was 'roughed' with emery paper, and later cleaned with Rubber Renue.

Both autostop, and take-up torque are now functioning correctly.


Shown here is the autostop at the point of being triggered.

It is worth noting that the autostop is only triggered for Play/RecPlay action, and not for rewind, or fast-forward operation.

If I have another criticism to make it is that the autostop will not be triggred if the take-up spool fails to turn, or lacks enough torque to turn the cassette tape reels.

Pinch Roller Tensioning - Again!

I finally decided to return the torsion spring back to its intended postion. I was always aware that its new postion could cause some small mechanical intereference.

The task was made easier by first bending (deforming) the torsion spring until it formed a new starting point angle. This means that the effective spring torque when setup would be less, but no less sufficient.


This made the return of the spring easier, but not easy! To keep the spring under control, I employed two pieces of tied string to keep the torsion spring stable in its position until I was able to release the long end into its target anchor point.




New Drive Belt

The previous drive belt measured approximately 86mm in diameter, and 3.5mm in width.
 
I fitted a few belts of different diameters and widths, but for better performance an 82mm diameter x 3mm width was best, and yielded the lowest (so far) wow and flutter figures. Wow & Flutter is averaging at 0.11% weighted rms (Japanese Standard JIS) figures.

The latest 0.11% wrms figure in green was achieved after the DC motor had been disassembled and cleaned with Servisol Super 10. The earlier figure in red was before the DC motor was cleaned, and also includes a larger 85mm x 5mm wide belt.

Initial Wow & Flutter Figures
with New Belts

 
Clearly the better figures are in green, but a noticeable trend of increasing wow and flutter was noted over this approximately 9 minute period. This will be investigated later.

Playback Sporadic Oscillation


There were sporadic oscillations of high frequency, mainly in the left channel on playback. The exact cause of this is uncertain, but applying switch cleaner to the Play/Record multiswitch, and 'working' the Record ON mechanism solved the problem. Since then, oscillations have only occasionally returned, but are soon stopped once the Record multiswitch is 'worked' again. 
 
Record-Play Switch
 
A serious attempt was made to stop these occasional bursts of instability, and so the record/play switch had to be completely disassembled as one line of enquiry.

This was de-soldered from the main audio board using a de-soldering station. Make no mistake, this is quite a time-consuming job.
 
In the end, the result was positive, so far - no more oscillations.
 
Switch removed from Main Board

Component Side with Switch Removed

After careful disassembly.

Contacts - All Cleaned.

Record-Play Multiswitch Ready!

Switch Returned to the Main Board

Bias Notes

On the front panel of the RS-630TUS deck are switches for bias and equalisation. It is quite easy to select a high bias for a Normal (Type I) tape, but of course using the default 120µS playback equalisation, or a 1326Hz 'Corner Frequency'. 
 
Currently, with the deck in its present state, a high bias record setting gives a frequency response from 30Hz to 14Khz at -3dB at either end, reference 0dB at 1Khz, from a TDK D46 Type I tape.

The selected high bias switch is insufficient for Chrome or Type II tapes in my opinion - there is too much distortion, any Chrome tape on this machine will be under-biased. I shall modify the circuit later and report back on this.

Front Panel Switches: Dolby/Bias/EQ/VU Metering

It was obvious that the action of the VU peak meter switching was inconsistent, and as a precaution since this deck is old, all four DPDT switches were removed. First desoldered, disassembled, and cleaned of long time oxidation and and accumulation of dirt.

Before de-soldering

Switch taken apart.


All four switches returned

 
Re-Capping

So far only the power supply unit and those electrolytic capacitors involved with the VU meters have been updated.

DC Motor & Controller

The DC motor and its controller circuit was opened up again, this time the brush and commutator design was investigated.

The commutator is a a little unconventional for this type of motor - in my opinion better than other simple DC motor designs. Here both commutator and brushes were cleaned, the former was cleaned first with a Q-Tip and switch cleaner, but later on with a little metal polish, then 'finished off' with switch cleaner again. Both ends of the motor shafts were lightly oiled.



A KSC1815-GR replaced the 2SC828,
for no ther reason that the 2SC828 was old.

The remaining 'power transistor' outside of
the motor with heatsink is a 2SB324 (PNP Germanium!)
The 2SB324 has not yet been replaced.

One electroltic capacitor was replaced.

The single blue tantalum bead cap of 100nF tested good.


Revised Wow & Flutter Figures

I was curious to see if any improvement could be made to the previous wow & flutter figures? To my pleasant surprise wow & flutter was reduced to a mean value of about 0.097% (JIS WRMS).




Speed Stability Revised

Casually, speed drift was examine over a period of about 14 minutes. Very pleasing results so far.



{Article unfinished, and also subject to changes and corrections.
16/10/2024}



Additional Pictures ...









Monday, 26 August 2024

Sanyo RD 4600 - Direct Drive Capstan Cassette Deck

Sanyo RD 4600



Advertised on ebay (uk) as not working I won the bid and took my chance with this purchase.

I could see that the VU meters were problematic, and indeed upon opening up the meter casing I could identify that the left channel VU meter had its loading/return spring partially buckled.

An attempt was made to salvage the VU meter by very carefully de-buckling the return spring and then strengthening the weak area with ultraviolet light glue - the process worked very well. So now both meters work.

The VU Meters before they were partially repaired.

Initial Findings
 

Before any work on the meters was done, the machine arrived near 'dead' - the meter lamps lit up, but nothing else happened.

For anyone not familiar with the RD 4600, I'll issue a warning - this cassette deck is not 'repair friendly'. It took me some time to decipher how open up the machine.


Power Supply Unit

Observing the PSU, it was noted that a push-on cable had come away and returning this to its intended point, the motor began to rotate! At last, the deck was 'alive'.

At this point the deck would playback tapes, although take up spool  torque was low, and RW/FF didn't work consistently. These faults were soon taken care of via disassembly of the cassette transport and cleaning.

The next and obvious job was to re-populate the PSU with new electrolytic capacitors.


Sanyo RD 4600 PSU, and Bias Oscillator Board.
Image shows the unit partially re-capped.
Later - many of the other components were
also replaced.


This board not only acts as a power supply unit (PSU), but also for two sources of DC supply voltage - a regulated supply at about 19v, and nonregulated at about 24v.

The said board also contains the bias oscillator, bias current control to match bias to the tapes, and a bias trap. The purpose of the trap is to filter out the bias high frequency and relatively high bias voltage from the audio circuits.


Play Mode

In PLAY mode, the deck would sometimes not operate - one source of this problem was a sticky PLAY solenoid. All mechanisms were cleaned with IPA and a Servisol Super 10 equivalent.

Another issue that surfaced was that pressing PLAY didn't always activate the full driving voltage (approx 12v DC) across the solenoid to operate the PLAY mechanism. I originally thought there may be a problem with the solenoid, but it transpired that the PLAY relay internal contacts were probably and partially corroded? All relays associated with Record/Play/Pause/Cassette-Eject were replaced.

To identify this, studying the service manual's circuit diagram was neccessary and the returned hypothesis was that relay contacts were probably to blame.

 


The DC driving voltage for the PLAY solenoid is approximately 12v, but under load conditions this didn't happen? My thinking was that - the relay contacts were offering (internally) high impedance to the circuit. This explained why the solenoid did not activate - too much voltage drop across the corroded contacts, hence not enough current to drive the solenoid.

RD 4600 with New OMRON G5LE-14 relays


Record Bias Noise in Right Channel

The original head recorded and played back fine, no problems except that there was low-level, but noticeable random bursts of extra white/pink noise (bias noise) in the right channel.

After studying most or all of the possibilities, it was concluded that the original Sanyo head was faulty; quite why it did this I don't know?, but similar occurances have happened to other hard-wearing heads like - the Sony Ferrite & Ferrite heads.

Gap erosion is a subject that is talked about on the Tapeheads forum, and I'm assuming that this just might be one of the negative 'spin offs' from this?

I was reluctant to swap the head, but I did eventually. The replacement was a (Chinese made?) DYNY62.


Estimation of Record Head Bias Current

Firstly we measure head inductances, the general consensus seems to be - measure at 10Khz, so we have ...

  • Sanyo T-159 D5A5: Right~165.8mH, Left~163.2mH.
  • DYNY62: Right~126.7mH, Left~120.5mH.

From this, the head impedance, and hence AC bias current generated at the bias operating frequency of 100Khz can be estimated.

Making the assumption that bias voltage is about 15v to 20v rms, then ...

From basic Ohm's Law: I = V/Z(𝟂), where the impedance Z(𝟂) is almost exclusively inductive, we can estimate the impedance due to the inductive reactance X at 100,000Hz, and later the bias current.

Bias Current: I ≅ V/X

But X = 𝟂L = 2πfL = 2x3.14159x10^5*L

Where L is the inductance in Henries. 

Then for Sanyo (Right Channel) ...

15/(2πx10^5*0.166) to 20
/(2πx10^5*0.166), or 144µA to 192µA.

And for DYNY62 (Right Channel) ...

15/(2πx10^5*0.127) to 20
/(2πx10^5*0.127), or 188µA to 251µA.


These bias current are low by default and comparing, they are not radically different.

The effective impedances at audio frequencies will be much less, but so too will the audio signals. Typically, audio AC voltage signals will be in the
µV range, and possibly a few mV at higher frequencies due to recording pre-emphasis.

Original Sanyo T-159 D5A5 Record/PB Head.


New Head in Circuit.

New DYNY62 REC/PB Head During Testing

Fitting the head was not so simple, the original Sanyo head and platform screw holes are postioned differently from other 'standard' two-head cassette decks. The rightmost new head's guide hole had to be elongated by about 1mm before a near centre line for the head could be established. In fact, more work may be done on this later. Head penetration is unaffected.

Wow & Flutter (Initial tests)

With the original pinch roller, wow & flutter figures as measured by WFGUI indicate figures almost consistently under 0.08% wrms.


TDK D46 Initial Tests


These indicate the record/playback frequency response at -20dB (ref: 0VU) is better than 40Hz to 15,500Khz (±3dB). And Total Harmonic Distortion at +6dB (Ref: 0VU) in the region of 1%. (I will update these figures when the machine is considered to be completely restored)

Before a 'new' head was fitted, the audio board was almost completely re-capped, and most of the original NPN and PNP transistors were replaced by KSA1845-FTA/C1815-GR/2SA992/2SC2001 types where required.

Work was be done on a soft surface
to avoid damages and scratches.
Here I've used an old clean carpet mat.


Main Audio Board.
Also, the mains transformer area is highlighted,
and adjacent pre-emphasis circuit.
(See comment below)

Warning: while the electronic design is very good, the audio board layout is poor in my opinion - too many components in such a small area made de-soldering difficult. Sanyo obviously just wanted these units sold!

It is recommended that anyone undertaking such work must use an efficient and accurate de-soldering gun/station.

Azimuth and playback levels were also calibrated from ABEX/TEAC full track reference tapes. Track height was not investigated, the new and old heads appear to have the same base thickness? Recording and playback to and from other third party machines was satisfactory - no obvious azimuth issues or instabilities.

Tape Type Provisions

The RD 4800 appears to have no provision for high bias tapes, like that of a typical Type II tape. Switching in 'CrO2' on the deck only alters pre-emphasis and de-emphasis; it does not increase bias.

No further testing has yet been done on any 'CrO2' or Type II tape.

Other Refinements Pending -

(1) Extra Transformer Shielding. 

Stray 50Hz electromagnetic fields appear to be picked up in the right channel of the recording circuit (but not playback), and I suspect probably during pre-emphasis, as this section is adjacent to the transformer as indicated above.

Observing Fast Fourier Transform plots on the playback noise (tape hiss) the interference is low, it mainly consists of odd-numbered harmonics of 50Hz (ie, 150Hz, 250Hz, 350Hz), but can be heard during very quiet passages.


(2) Higher than expect bass distortion - @50Hz, at 0VU record/playback, THD ~ 3%.

(3) New VU Meter Lighting.

(4) Pre-emphasis tweaking, otherwise known as 'Record EQ'.

Currently, the 'Standard' setting sets more pre-emphasis (ie, high frequency 'lift' above 400Hz) than the 'Low Noise' tape setting - this is not necessarily incorrect.

It is interesting when studying the circuit diagrams to see Sanyo allowing tweaking of pre-emphasis via ferrite cored inductor trimmers and one trimmer resistor for the 'Standard' tape setting.

With the new head in circuit, there is a high frequency rise of about 2dB/3dB starting above 10Khz which drops back to 1,000Hz levels at 15,000Hz.

Fall off after 15,000hz is rapid due to the limitations of the head, tape, tape speed, and restrictions applied from the FM multiplex filter. This rise may be 'smoothed out' if the pre-emphasis 'reasonant' frequency was moved to a higher point, and the associated in-series resistor increased to 'dampen' the Q-factor?

In the circuit below, ferrite core inductor trimmers L102/L103/L104 are adjustable and will alter the resonant frequency of the respective 'series' circuit. Capacitors too can be altered to change the 'resonant' frequency; circuit not yet tested).



From memory, the original Sanyo head returned similar frequency response results.

(4) Peak Level Lighting

Peak levels are often set at around +5dB to +6dB above 0VU, but in the case of this Sanyo, we have a sitiation where the response of a peak is slow, due the nature of the filament lamp. A better solution would be to employ an LED circuit, which is visibly faster acting.

Currently peak indication is set to 0VU, from which I estimate the actual peak is somewhere around +6dB above 0VU. This seems to be a sensible setting for this machine.

Summary

So here is the Sanyo RD 4600 after 35-40 hours work on it, and returned back to its case.

A very classy looking retro deck! However, there is more work to do on this machine.





These photographs were taken
using long exposure photography.

Refinements: Frequency Response

So back to some of the pending issues, we begin with record-playback frequency response.

With regard to tweaking the pre-emphasis as mentioned above, I increased the value of R319/R419 from 100 ohms to 150 ohms in an attempt to 'dampen' the peak rise above 10Khz. This has partially worked, and after reducing the bias a little, a quick and rather convenient assessment of the Sanyo record-playback frequency response was sought employing FFT on the application of White Noise at approximately -20dB, reference 0VU. The FFT plot is not ideal, but gives a good indication of the ability of the Sanyo.


Taking 1,000Hz as reference, there is deviation of -1dB at 10Khz, which then rises to about +2dB before settling back to 15,500Hz at -3dB. On the bass side, we see that at about 35Hz/36Hz, there is a -3dB drop.

A further reduction bias would raise the 10Khz level a little more, but I ran out of potentiometer resistance!

The electromagnetic interference discussed earlier is noticeable at this -20dB plot, in particular the dominant 150hz peak mainly in the right channel illustrated in red. A noise artefact at 20Hz also appears, quite where this comes from I do not know, but possibly from the brushless DC motor?

Low Frequency Audio Distortion

An irritating, but not-so-obvious problem with the audio was the low-frequency audio distortion that I percieved during subjective listening tests. This manifested itself as 'muddy' sound.

Several ideas came to mind as to the potential sources of this unwanted sound artefact. They were - (a) improper PB pre-amplifier biasing, (b) faulty muting transistors, (c) the record-playback multiswitch, or (d) the record head.

My first attack was to eliminate (c), the record-playback multiswitch. I knew this was going to be a risk when attempting to resolve the issue.

This 26-holed switch was very carefully de-soldered using a suction-based de-soldering station, and then removed from the board. The circuit board was then cleaned, but the job of opening up the switches (L-ch and R-ch) was a little intimidating - they are so easy to break.

With thoughtful and careful application, the job of cleaning or re-newing these two switches was done.


Record-Playback Switches After Removal from Circuit Board.


Disassembled Record-PB Multiswitch


Contacts Cleaned in Vice.


Before Re-assembly, then
Returning the Switches
to the Audio Board
 

Cleaned Audio Board


Multiswitches for Left and Right Channel -
Resoldered into Audio Board.
Full circuit board clean was done later.

Some 3 hours of work went into the job, but the improvement was only slight.

Next on the list of possible sources of the 'muddy sound' were the muting transistors

Labelled as Q114/Q214 on the schematic, these were initially replaced by 2SC2001. The thought had crossed my mind that I may have inserted the said transistors incorrectly?, but not according to the board layout as described in the service manual. Nor did I doubt the 'pinout' schematic for the 2SC2001 NPN transistors.

With the muting transistors removed, I went throught the process again of testing the sound.

Result? - postive!, no more muddy bass sound, no more mild mid-range 'stress' and treble came to life!



Distorton Figures


Tape: TDK C-46

Again, returning to the spectrum FFT plots, distortion at record/playback at Dolby level was re-estimated.

Third Harmonic Distortion is commonly defined by ...



At 100Hz at Dolby Level


Only two harmonics of the fundermental in question were taken, since the affects of remaining spectra are negligible. The relative differences  of the harmonics were estimated using FFT analysis.



At 1000Hz at Dolby Level




Leaking Transformer Interference

So far, a lot of work has gone into restoring the RD 4600, and although the mild right channel 'hum' (150Hz third harmonic) is a subject to be addressed, essential work on this deck is considered to be finished, at least as far as this blogger article is concerned. If and when additional shielding around the transformer is complete, this will be updated below. (03/09/2024)

Brushless DC Motor Assessment

After finishing returning the filament lamps to the VU meters, the brushless dc motor was examined. Of interest to the reader, here are some photographs.




The Brushless DC Motor






Pre-Emphasis Changes to 'Standard' Tapes

In the pre-emphasis or Record-EQ circuit, the 'Standard' setting is now configured so that it is now electrically the same as the 'Low Noise' setting internally. 

Previously the 'Standard' tape pre-emphasis was much greater than the 'Low Noise' setting, which forced a much higher high frequency rise during record (pre-emphasis), thus returning an uneven frequency response. Overall frequency response is now much flatter, but not identical - the Low Noise setting still shows the an after-10Khz rise (see above), while the new 'Standard' setting shows a dip around 10Khz of about 0.5dB to 1dB. Both settings can still be 'tweaked' using the relevant ferrite cored trimmer inductors.

Power Supply Fusing

While the service manual suggests in its schematic a full set of secondary fuses to protect the deck, there were no fuses to be found in this UK model!?


A suitable solution will be found later.

Secondary Transformer Cables.
No fuses found on this machine!



Fuse Solution


Three 20mm fuses holders were later inserted into the power supply circuit. These holders were placed electrically into the secondary side of the transformer.


Later I realised that the middle '800mA' fuse holder was not required, I had made a mistake, so the fuse was removed and the line reconnected within.


AC Transformer Secondary Winding Fuses -

2000mA Orange:
In line fuse for the unregulated DC power supply for the DC motor, and relays.
800mA Yellow: In line fuse for the regulated
DC power supply for the audio.

The fuse holders were later tied, and 'tidied up'.

Calibration Labelling


cassettedeckman@gmail.com

(Note: The Blogger editor is full of bugs, and so making editing very difficult at times. For this reason you may see the occasional unusual formatting.)

This article is in principle - finished, but small additions and corrections are still possible. (15/09/2024)